EPSON STYLUS PRO 10000
ERROR CODES
SERVICE
CALL 00,010,015: INK SURFACE SENSOR (K) OVERFLOW
Surface of a liquid sensor defective or I/C valve
solenoid defective it is (on condition).
• I/C valve solenoid exchange
• C362DRV board exchange
•
Surface of a liquid sensor exchanger
SERVICE
CALL 00,010,016: INK SURFACE SENSOR (C) OVERFLOW
Surface of a liquid sensor defective or I/C valve
solenoid defective it is (on condition).
• I/C valve solenoid exchange
• C362DRV board exchange
•
Surface of a liquid sensor exchanger
SERVICE
CALL 00,010,017: INK SURFACE SENSOR (M) OVERFLOW
Surface of a liquid sensor defective or I/C valve
solenoid defective it is (on condition).
• I/C valve solenoid exchange
• C362DRV board exchange
•
Surface of a liquid sensor exchanger
SERVICE
CALL 00,010,018: INK SURFACE SENSOR (LC) OVERFLOW
Surface of a liquid sensor defective or I/C valve
solenoid defective it is (on condition).
• I/C valve solenoid exchange
• C362DRV board exchange
•
Surface of a liquid sensor exchanger
SERVICE
CALL 00,010,019: INK SURFACE SENSOR (LM) OVERFLOW
Surface of a liquid sensor defective or I/C valve
solenoid defective it is (on condition).
• I/C valve solenoid exchange
• C362DRV board exchange
•
Surface of a liquid sensor exchanger
SERVICE
CALL 00000100:Waste ink tank full
The waste ink pads are completely full, causing a fatal
error. The printer stops printing.
It is similar as "Maintenance call 0100".
SERVICE
CALL 00000101: CR motor life (Even Ink tube life)
The carriage drive system reached the life.
The following confirmation and also part exchange and CR
motor initialization
• Whether there is not ink leakage from the ink supply
tube and also coupling department, is confirmed.
• It confirms whether there
are not dirt and abrasion in the slowing-down gear that was attached to the CR
timing belt, PF roller axis.
• The CR timing belt tension confirms whether or
not it is normal.
• Exchange the CR motor and ink tube. After the above part
are exchanged, "CR motor Initialization" of maintenance mode 2 is
run.
SERVICE
CALL 00000102 :Waste ink box on the right side full
It is ’00,000,100’ and time in the detailed that
displayed it to the LCD panel and be not fatal error
Not necessary ("Waste ink Initialization" of
maintenance mode 2 is run.)
SERVICE
CALL 00000103 : Waste ink box on the left side full
It is ’00,000,100’ and time in the detailed that
displayed it to the LCD panel and be not fatal error.
Not necessary ("Waste ink Initialization" of
maintenance mode 2 is run.)
SERVICE
CALL 00010000: PF ENCODER CHECK ERROR
PF motor encoder check error The PF motor makes small
revolutions clockwise and counter-clockwise. When it turns, the printer checks
the rotary encoder (inside the motor) output signals to make sure the motor is
turning at the correct speed/distance. If the encoder sends an incorrect
signal, an error occurs.
Make sure there is nothing blocking the grid rollers. If
that does not solve the problem, check the PF motor encoder connection. If
there still is a problem, carry out the tension adjustment or phenol-formaldehyde
motor exchange of the phenol-formaldehyde timing belt. If there is not a
problem, carry out the following items.
• Confirming whether the dirt and dust
are not adhering to the PF loop scale and PF encoder.
• The cable connector
joint of the PF encoder and C362DRV board (CN8) are confirmed.
• The PF timing
belt tension confirmation/adjustment. In the case that there is not abnormality
with above checking I gradually exchange the next part.
• PF encoder
• PF
timing belt
• PF loop scale
• PF encoder extension cable
• C362DRV board
SERVICE
CALL 00010001: PF MOTOR STEP-OUT
PF motor out of step - the length of the PF motor
internal encoder’s pulse is too long or too short compared to the regular
pulse.
Make sure there is nothing blocking the grid rollers. If
that does not solve the problem, check the PF motor encoder connection. If
there still is a problem, try the following. • PF timing belt exchange
• PF
motor exchange
• PF motor extension cable exchange
• C362DRV board exchange.
SERVICE
CALL 00010002: PF MOTOR OVER CURRENT
PF motor overcurrent - Feedback from the PF motor (IC35)
driver’s 10-pin output (sensor signal) indicates that the PF motor’s current is
irregular.
• The coil resistance value (6.7Ohm) the measurement of
the PF motor.
• PF motor extension cable exchange.
• C362DRV board exchange.
SERVICE
CALL 00010003: PF MOTOR IN POSITION TIME OUT
When be it locateds stable at the time of halt processing
with the PF motor control, (the in position time) the position control inside
period did not improve
• PF motor exchange
• PF encoder exchange
• PF timing
belt exchange
• C362DRV board exchange
SERVICE
CALL 00010004: CR ENCODER CHECKING ERROR
CR motor encoder check error The CR motor makes small
revolutions clockwise and counter-clockwise.When it turns, the printer checks
the encoder output signals to make sure the motor is turning at the correct
speed/distance. If the encoder doesn’t send the correct signal or output data,
an error occurs.
It confirms whether there is not abnormal load etc. at
the time of carriage migration and be abnormal no and do the checking of the CR
encoder, in the case that the error is not canceled. In the case that there is
abnormality : Carry out the tension of the steel belt adjustment or CR motor
exchange. In the case that there is not abnormality : Confirm whether there are
not dirt and damage in the CR encoder. The cable connector joint to the CR
encoder and head Assy board CN15 are confirmed. Encoder pulse detection for T
fence (scale 180a) of it comes off/whether or not there is not the contact with
a CR encoder
• Confirmation of the dirt/paper powder/damage of the confirmation
T fence (scale 180a) the top
• CR encoder exchange
• CR motor exchange
•
C362DRV board exchange
SERVICE
CALL 00010005: CR MOTOR STEP-OUT
The rotational speed of the CR motor abnormal. (it is
long/short period at the time of prescription ).
It confirms whether there is not abnormal load etc. at
the time of carriage migration and be abnormal no and do the checking of the CR
encoder, in the case that the error is not canceled. In the case that there is
abnormality:
• Encoder pulse detection for T fence (scale 180a) of it comes
off/whether or not there is not the contact with a CR encoder
• Tension
adjustment of the confirmation steel belt
• Confirmation of the dirt / paper
powder / damage of the T fence (scale 180a) the top
• CR encoder exchange
• CR
motor exchange
• C362DRV board exchange